|
July 3, 2002
Mr. John A. Grobe, Chairman
Davis-Besse 0350 Panel
United States Nuclear Regulatory Commission
801 Warrenville Road
Lisle, IL 60532-4351
Mr. Edwin M. Hackett, Assistant Team Leader
Davis-Besse Reactor Vessel Head Degradation Lesson-Learned Task Force
United States Nuclear Regulatory Commission
Washington, DC 20555-0001
Dear Mr. Grobe and Mr. Hackett:
The Union of Concerned Scientists (UCS) continues to examine the Davis-Besse
near-miss loss-of-coolant-accident. We recently obtained a number of
documents
from the NRC's Public Document Room that shed additional light on the
matter. In case our review doesn't cover ground you have already been over,
we are
passing along things we have discovered to the Davis-Besse 0350 Panel and
the Lessons Learned Task Force. We have not enclosed the source documents.
Since
we obtained them from the NRC's Public Document Room, we assume that they
are readily available to you. If you have any problems fetching the
documents,
let me know and I can send along copies.
What does the NRC mean by "acceptable"?
In its Final Root Cause Report dated April 18, 2002, First Energy reported
that the NRC had inspected the boric acid corrosion program at Davis-Besse
and
judged it acceptable. This conclusion appears to have been based on this NRC
statement:
"The purpose of this letter is to advise you that our audit of your boric
acid corrosion prevention program has resulted in an acceptable finding and
we
now consider this issue to be closed."
[1]
The NRC sent two NRC staffers and a consultant from Brookhaven National
Laboratory to Davis-Besse between September 11-13, 1989. The report issued
following
their inspection did indeed contain the aforementioned "acceptable"
statement, but it also contained this statement:
"The following areas of boric acid corrosion prevention could be enhanced at
the Davis-Besse plant:
a) System and operations engineers who perform boric acid leak
inspections should have some formal training prior to performing the
inspections.
b) Inspections performed by the system and operations staff should
be documented formally."
The consultant who accompanied the NRC inspectors to Davis-Besse and nine
other nuclear plants subsequently authored a report for the NRC. In that
report,
he stated:
"The plant audits showed a considerable variance in the mode and quality of
boric acid corrosion programs between utilities. The degree of importance of
a boric acid corrosion control program also varied considerably between
plants. In the plants where a reasonably high priority was given to the
problem,
the leaks were identified and corrective actions taken in a timely manner."
[2]
In Table 2 of his report, the consultant graded the boric acid corrosion
programs in nine areas. Davis-Besse was Plant #9 in his tabulation. He
assigned
Davis-Besse grades of "2" in the areas of "Procedure for Damage Evaluation"
and "Training of Inspectors." According to Section 5.3, "Evaluation of Audit
Results," a grade of "2" meant "Unsatisfactory." Only two plants received
lower overall scores than Davis-Besse. The majority of plants (seven)
received
better overall scores than Davis-Besse.
UCS was disappointed to discover that the NRC determined that two of nine
(22.2 percent) of the boric acid corrosion program elements were
unsatisfactory,
yet still accepted it. In fact, if we understand the consultant's report
correctly, Davis-Besse could have been graded "unsatisfactory" in all nine
elements
and still received an "acceptable" finding from the NRC. Talk about
unsatisfactory! The NRC did not ask, yet alone require, Davis-Besse to
remedy the
elements of its program determined to be unsatisfactory. In many ways, this
is worse than not knowing that their program was bad. The NRC knew it was
bad
and accepted it that way.
| UCS-09a |
Why did the NRC "accept" the boric acid corrosion program at Davis-Besse
after determining that over 20 percent of the program was "unsatisfactory"? |
| UCS-09b |
If the 0350 Panel determines that restart is "acceptable," will "acceptable"
rely on one or more NRC findings of "unsatisfactory" conditions at
Davis-Besse?
In other words, will "acceptable" and "unsatisfactory" stop being synonymous
to the NRC? |
How did Davis-Besse accomplish what Cher wanted to do, turn back time?
The NRC staff concluded its heightened regulatory efforts for the plant were
necessary as a "result of the series of problems that formed a long history
of ineffective and inadequate attention and direction in the operation and
maintenance of the Davis-Besse facility."
While this conclusion appears contemporary, it actually applied to a June 9,
1985, loss of feedwater event at Davis-Besse.
[3]
That event, according to the NRC, resulted in a conditional core damage
frequency of 3.6x10-2, an extraordinarily high risk given that other
near-misses
have values in the 1x10-5 to 1x10-7 range. In fact, the NRC reported that
only two other events at Babcock & Wilcox nuclear plants like Davis-Besse
had
as higher or higher risk in recorded history. Those events were a March 20,
1978, loss of power at the Rancho Seco nuclear plant in California
(permanently
shut down in the early 1990s due to safety and economic concerns) and a
September 9, 1977, loss of feedwater event at Davis-Besse. The 1977 event at
Davis-Besse
also had the extraordinarily high conditional core damage frequency of
3.6x10-2.
[4]
This was not surprising considering that it was the same event and the
company had done nothing to lessen the risk after the first near-miss.
As the NRC itself concluded, chronic and systemic management problems caused
the very, very serious near-miss at Davis-Besse in 1985. The NRC must share
some responsibility for that near-miss because it was a virtual repeat of a
1977 near-miss at Davis-Besse that the NRC tolerated without any upgrades at
the facility. The NRC must have concluded that the "unsatisfactory" 1977
near-miss was "acceptable" until lightning struck a second time in 1985.
As the company's root cause team concluded and NRC's AIT confirmed, chronic
and systemic management problems caused the very, very serious near-miss at
Davis-Besse in 2002. The NRC must share some responsibility for that
near-miss because the agency "accepted" a boric acid control program in 1990
that
it knew was "unsatisfactory" in over 20 percent of the areas evaluated.
| UCS-10a |
How many times must the people living around Davis-Besse be subjected to
American Roulette? |
| UCS-10b |
What tangible steps will NRC take to prevent chronic and systemic management
problems from causing yet another very, very serious near-miss-or worse-at
Davis-Besse? |
Why should anyone believe the NRC's Ouija Board?
As UCS documented two years ago,
[5]
the risk assessments performed for nuclear power plants are fundamentally
flawed. Among other deficiencies, the risk assessments assume there is a
negligible
chance of reactor vessel damage. UCS went to the NRC's Public Document Room
on June 28, 2002, to examine the plant-specific risk assessment for
Davis-Besse
submitted by the plant's owner in March 1993. We wanted to confirm that
potential reactor vessel damage had been downplayed in the Davis-Besse risk
assessment
as it had been in the dozen-plus risk assessments we have reviewed for other
nuclear plants. But UCS was denied access to this document by the NRC.
The Significance Determination Process (SDP) used by NRC to evaluate the
safety impact of the reactor vessel damage at Davis-Besse is almost
exclusively
based on the "secret" plant-specific risk assessment.
[6]
The NRC's SDP worksheets for Davis-Besse are 49 pages long, including the
transmittal letter, cover sheet, and table of contents. It refers to the
Davis-Besse
risk assessment approximately 43 separate times. In fact, it has only two
references: (1) the Davis-Besse risk assessment, and (2) NRC staff paper
SECY-99-007A
titled "Recommendations for Reactor Oversight Process Improvements
(Follow-up to SECY-99-007)." The SECY paper claimed that the new oversight
program would
be scrutable, transparent, and based on publicly available information. But
the NRC does not allow the public to look at the information it uses to
assign
safety significance to events. Shame on the agency! UCS would request that
the NRC staff revise SECY-99-007A to reflect its actual rather than intended
practices, but the agency would probably classify the revised document
"confidential" and hide it from the public, too.
UCS located a publicly-available, at least for the moment, document
addressing the treatment of reactor vessel damage:
[7]
Davis-Besse demonstrated the utter fallacy of assuming "stringent"
surveillance practices. That the reactor vessel at Davis-Besse did not fail
is due more
to luck than the skill of either the plant owner or the NRC. Reactor vessel
damage has occurred and will likely occur again. It is non-conservative and
just plain foolhardy to pretend that it will not. Someday, the good luck may
run out.
Yet the NRC used the flawed, deficient, and non-conservative risk assessment
last fall to justify deferral of the mandated inspection for CRDM nozzle
damage.
And it is this risk assessment that the NRC is now using to determine the
safety significance of the reactor vessel head damage at Davis-Besse. Yep,
the
agency is using a risk assessment specifically discounting reactor vessel
damage as a possibility to determine the significance of reactor vessel
damage.
That's at least two stops past absurd on the sheer folly train.
The NRC's revised reactor oversight program is allegedly risk-informed. It
purportedly uses risk insights to focus plant owner and NRC attention
towards
the most safety significant areas. For example, the plant-specific risk
assessments determine the importance of a system or component by calculating
the
chances of reactor core damage with and without it. The importance values
are then sorted to distinguish the highest risk systems/components from
those
having the least risk. The NRC's inspectors select systems and components
from the top of that list for their audits.
But because the risk assessments assume nearly a zero percent chance of
reactor vessel failure, the reactor vessel is not even on the list. It ain't
at
the top, it ain't at the bottom, it ain't on the list at all. Thus, even if
the NRC inspectors were to "bottom fish" and pick the least important
systems/components
on the list, they still will not audit the reactor vessel.
Yesterday, UCS found a 1999 update to the Davis-Besse risk assessment in the
NRC's ADAMS on-line library.
[8]
This document confirms our suspicions. The chances of reactor vessel failure
was deemed to be 4.5x10-7 per reactor year. By arbitrarily assigning an
artificially
low value that has no real basis, the reactor vessel did not even make the
list of risk significant systems and components. What made the list?
The math wizards at Davis-Besse report that the spare service water (SW)
pump has essentially no risk relevance, but it is still-according to their
goofy
Ouija board at least-far more important than the measly ol' reactor vessel
head. This hocus-pocus doesn't even pass the laugh test.
The fundamentally flawed risk assessments are more than mere mathematical
miscues. Their output is heavily relied upon by the NRC's revised reactor
oversight
program. The "garbage" produced by the fundamentally flawed risk assessments
thus corrupts the entire reactor oversight program. It prevents NRC
inspectors
from auditing reactor vessel integrity. It prevents NRC inspectors from
auditing ice-condensers. It prevents NRC inspectors from auditing other
areas non-conservatively
omitted from the risk assessments. It blinds NRC inspectors from adequately
protecting the American public from nuclear plant risks. It is
"unsatisfactory"
and "unacceptable" and "unjustifiable."
| UCS-11a |
Will the NRC allow the public to look at the 1993 Davis-Besse risk
assessment? |
|
UCS-11b |
Out of curiosity, why did the NRC staff use the old 1993 Davis-Besse risk
assessment to develop its Significance Determination Process worksheets when
the
updated 1999 plant safety assessment was readily available? Did the staff
prefer to use an old "secret" report instead of a recently updated version
that
the public could obtain? |
| UCS-11c |
If the Davis-Besse risk assessment remains "secret" but it the basis for the
SDP call, why should the public believe any NRC pronouncement on safety
significance
derived, in large part, on "secret" information? |
| UCS-11d |
If the Davis-Besse risk assessment remains "secret," will the NRC retain the
0350 Panel in place following restart indefinitely to compensate for the
public
being unfairly excluded from access to this key information? |
| UCS-11e |
Will the NRC require the Davis-Besse risk assessment to incorporate the real
risk from reactor vessel failure before the plant restarts? |
| UCS-11f |
When the NRC revamp its reactor oversight program to enable its inspectors
to audit areas non-conservatively omitted from the plant-specific risk
assessments? |
Did First Energy repeat Callaway's mistakes?
NRC Region IV cited the owner of the Callaway nuclear plant in Missouri with
a violation of occupational radiation exposure control requirements.
[9]
NRC Region IV was disenchanted because:
"As described in Section 2OS2 of this report, six jobs that accrued more
than 5 person-rems each during Refueling Outage 10 exceeded their projected
job
doses by more than 50 percent because of a number of performance problems."
Radiation Work Permit RWP 2000-5132 was written by plant workers at
Davis-Besse on April 6, 2000, to cover the vessel head cleaning task during
the 12th
refueling outage. It estimated a total job dose of 100 mRem. Due to various
performance problems encountered during the task (evidenced by Condition
Reports
CR 2000-0994 on April 16th, CR 2000-0995 on April 16th, and CR 2000-1037 on
April 17th, the estimated total job dose was revised upward again and again
to a final estimate of 600 mRem. RWP 2000-5132 was closed on April 25, 2000,
after the vessel head cleaning was completed. The total actual dose was 224
mRem, over 100 percent higher than the original guesstimate.
While 224 person-mRem is lower than 5-plus person-rem, Callaway and
Davis-Besse both experienced initial radiation exposure estimates
significantly below
actual radiation exposure estimates. The falsely low estimates impeded
informed decision-making on shielding, mock-ups, and other means of limiting
overall
worker exposures. In addition, part of the reason for the
higher-than-planned radiation exposures at Davis-Besse is the failure of
management to install
MOD 94-0025, which would have facilitated inspection and cleaning of the
reactor vessel head. The as-low-as-reasonably-achievable (ALARA) regulation
was
seemingly violated by First Energy's repeated decisions to defer MOD 94-0025
from outage to outage and allow workers to soak up radiation while
struggling
to inspect and clean the reactor vessel head.
And it's not like Davis-Besse has an exemplary radiation protection program.
If media accounts are accurate, contract workers at Davis-Besse carried
little
radioactive "souvenirs" with them to contaminate apartments and motels
across the US of A.
| UCS-12a |
Did First Energy violate the ALARA regulation by repeatedly deferring MOD
94-0025? |
| UCS-12b |
Does NRC Region III have a different approach to worker radiation safety
than NRC Region IV, given the fact that Callaway was cited for the same poor
radiation
control practices that Region III let Davis-Besse get away with? |
Is First Energy merely recycling excuses and promises?
As you know, I attended two of the three public meetings conducted by the
NRC in Oak Harbor, Ohio on June 12, 2002. I heard Mr. Lew Myers and Mr.
Randy
Fast of First Energy repeatedly speak of the need to catch up to the rest of
the industry. Mr. Fast outlined more than once a scheme to bench-mark
programs
at Davis-Besse against the industry's best. Mr Myers, on at least two
occasions, remarked that his operators needed to break their silence when
they notice
leaks and problems inside containment.
This all sounds really nice. It also sounded really nice all the times we've
heard it in the past. The company needs to back up its words with deeds.
After
the company missed several opportunities to figure out that boric acid
corrosion was damaging valve RC-2 inside containment in 1999, First Energy
informed
the NRC:
"As noted in the IR [NRC inspection report], following the determination
that boric acid corrosion was the most likely cause for the missing nuts on
the
body-to-bonnet bolting of valve RC-2, a thorough evaluation of the issue was
conducted and extensive, effective corrective actions were developed.
Greater
sensitivity to the effects of boric acid corrosion on plant equipment were
noted in the IR and integration of these insights into plant processes and
operational
philosophy are being institutionalized by: 1) developing a revision to the
Boric Acid control program and the Work Process Guidelines on plant leakage,
including the benchmarking of industry standards and practices, to reflect
higher standards for monitoring, evaluating, documenting and controlling
boric
acid leakage; and, 2) providing additional training to management and the
technical staff to address the technical issues of boric acid control, the
DBNPS
Boric Acid Control Program and requirements, lessons learned from the RC-2
event, and industry experience. We will continue to stress the use of a
questioning
attitude and conservative decision-making in managing and resolving
identified issues."
[10]
[emphasis added by UCS here, but apparently not by First Energy there]
Prior to joining UCS, I worked as a consultant on PSE&G's Salem 2 restart
project in 1995/1996. Salem was then in the regulatory doghouse for
non-conservative
decision-making. To roll out expectations on questioning attitude and
conservative decision-making, PSE&G instituted many measures to back up the
really
nice slogans it sent to NRC. For example, senior managers conducted a series
of informal luncheons with first-line supervisors and workers. To complement
training sessions, PSE&G added a column titled "Catch of the Week" to its
weekly employee newsletter highlighting issues raised by workers. This
attention
not only reinforced to workers that management did indeed want to hear about
problems, but it also helped calibrate workers to the important threshold
question for reporting problems. In short, PSE&G backed up its nice-sounding
words with meaningful, tangible actions.
| UCS-13 |
What tangible actions has First Energy taken to back up its rosy
proclamations and assertions about "questioning attitude and conservative
decision-making"? |
Will the NRC enforce existing regulations?
The NRC recently reported that "the licensee for Davis-Besse did not have a
regulatory commitment to clean the reactor pressure vessel (RPV) head."
[11]
UCS is more than a little baffled by this announcement. To be perfectly
frank, we do not believe it to be true. During the NRC public meeting
conducted
in the Commissioner's Auditorium on March 20, 2002, UCS presented
information to the NRC staff. Among that material (which only consisted of
five pages
so it should not have been overwhelming) was this statement:
Davis-Besse UFSAR Section 5.2.3.2, Materials Exposed to Reactor Coolant,
page 5.2-15 states "All materials exposed to the reactor coolant exhibit
corrosion
resistance for the expected service condition. . Sensitized stainless steel
weld overlay (cladding) is permitted."
Lest anyone think we "cut and paste" words out of context to suit our
purposes, here's the precise wording from the UFSAR itself:
The carbon steel exterior surface of the reactor vessel head is neither
corrosion-resistant nor clad with stainless steel. Thus, when highly
corrosive boric
acid crystals were discovered on this surface, the Davis-Besse UFSAR-as an
absolute minimum-required it to be cleaned. After all, it was clearly
material
exposed to reactor coolant. The existing Davis-Besse design and licensing
bases clearly and unequivocally require boric acid to be cleaned off the
reactor
vessel head. If First Energy, for whatever reason, wanted to leave the boric
acid on the exterior surface of the reactor vessel head, they had to either
comply with the requirements in UFSAR Section 5.2.3.2 or legally change it.
Ignoring that requirement year after year should not have been an option.
| UCS-14a |
Will the NRC require First Energy to conform with UFSAR Section 5.2.3.2 or
revise UFSAR Section 5.2.3.2 to match what the company does about boric acid
before restart? |
| UCS-14b |
If the NRC truly believes that First Energy, or any other nuclear plant
owner, lacks a regulatory commitment to clean the reactor vessel head of
highly
corrosive material that can cause catastrophic failure, shouldn't the agency
undertake as Job #1 getting that regulatory commitment? If not, why not? |
The discovery of significant reactor vessel head damage occurring as a
result of years of neglect would seem to undermine confidence in both the
plant owner
and the NRC. But it doesn't have to yield that result. The company and the
NRC could demonstrate with deeds rather than words that this is a learning
opportunity.
Or they could sustain the business-as-usual attitudes that created this
near-disaster by accepting unsatisfactory conditions and blithely dismissing
true
safety hazards. We hope for the former but will be monitoring closely for
signs of the latter.
Sincerely,
David Lochbaum
Nuclear Safety Engineer
Washington Office
Union of Concerned Scientists
Footnotes
-
Thomas V. Wambach, Senior, Project Manager - Project Directorate III-3,
Office of Nuclear Reactor Regulation, Nuclear Regulatory Commission, to
Donald C.
Shelton, Vice President - Nuclear, Toledo Edison Company, "Prevention of
Boric Acid Corrosion at Davis-Besse Nuclear Power Plant (Generic Letter
88-05),
(TAC No. 68915)," February 8, 1990.
-
C. J. Czajkowski, Brookhaven National Laboratory, "Survey of Boric Acid
Corrosion of Carbon Steel Components in Nuclear Plants," NUREG/CR-5576, June
1990.
-
Nuclear Regulatory Commission, Press Release No. 87-24, "NRC Staff Reduces
$900,000 Fine Against Davis-Besse by $450,000," February 12, 1987.
-
Nuclear Regulatory Commission, NUREG-1231, "Safety Evaluation Report related
to Babcock & Wilcox Owners Group Plant Reassessment Program," November 1987.
-
David Lochbaum, Union of Concerned Scientists, "Nuclear Plant Risk Studies:
Failing the Grade," August 2000.
-
Douglas V. Pickett, Senior Project Manager, Nuclear Regulatory Commission,
to Guy C. Campbell, Vice President - Nuclear, First Energy Nuclear Operating
Company, "Davis-Besse Nuclear Power Station - Site-Specific Worksheets For
Use in the Nuclear Regulatory Commission's Significance Determination
Process,"
March 14, 2000.
-
Nuclear Regulatory Commission, NUREG/CR-6042 Rev. 2, "Perspectives on
Reactor Safety."
-
Probabilistic Risk Assessment Unit, Design Basis Engineering, First Energy
Nuclear Operating Company, "Probabilistic Safety Assessment for the
Davis-Besse
Nuclear Power Station," October 1999.
-
Arthur T. Howell, III, Director - Division of Reactor Safety, Nuclear
Regulatory Commission, to Garry L. Randolph, Vice President and Chief
Nuclear Officer,
Union Electric Company, "Callaway Plant -- NRC Inspection Report No.
50-483/00-17," October 4, 2000.
-
Guy C. Campbell, Vice President - Nuclear, First Energy Nuclear Operating
Company, to Nuclear Regulatory Commission, "Response to Inspection Report
Number
50-346/98021 (DRP)," July 1, 1999.
-
Anthony J. Mendiola, Chief - Section 2 Project Directorate III, Nuclear
Regulatory Commission, to Paul M. Blanch, June 19, 2002.
|