CLEAR
22°
more weather




Thursday,
December 05, 2002

 



Tips on searching


Browse Last 30 Days
The Blade Archives
AP Archives


Latest News
Sports
Business
Arts & Entertainment
Davis-Besse In-depth
Opinion
Religion
Health & Science
Columnists
Obituaries
Special Reports
Weather
AP Wire
Photos of the Day
Lottery


General
Homes
Autos
Jobs
Boats/Recreation
Celebrations
Legal Notices
Directory of Worship
Personals

Events Calendar
Educational Services
Directories
Forums
E-thepeople
TV Listings
Movie Showtimes
Horoscopes


toledo
HBA Parade of Homes
Contests
KidZone
Mud Hens Web Cam


Set As Homepage
Subscriber Services
Email Newsletter
The Blade e-edition
Advertise
About Us
Contact Us
Help & FAQs

Regional News | Article published Thursday, December 5, 2002
DAVIS-BESSE
Regulators clueless to leak extent
After year, NRC explains delay in shutdown order

By TOM HENRY
BLADE STAFF WRITER


OAK HARBOR - Senior Nuclear Regulatory Commission officials suspected there might be minor leakage on the reactor head at the Davis-Besse nuclear plant, but they rejected a staff recommendation that the plant shut down immediately late last year because they considered the public risk "acceptably small," according to a report released yesterday.

In hindsight, the agency has repeatedly admitted, it was caught off guard by the magnitude of the what was found during an inspection after the reactor was shut down Feb. 16 for refueling: the most serious corrosion ever seen on a reactor head in the United States.

The extent of the damage was so severe that the NRC and other nuclear experts have since concluded that deterioration at Davis-Besse was the nation’s closest brush with a major nuclear accident since Three Mile Island in 1979.

Davis-Besse’s carbon steel reactor head had been eaten away in one-half-foot area to the point that only a stainless steel liner less than a quarter of an inch thick had prevented a disastrous leak of the reactor’s radioactive steam into the concrete containment building - the last line of defense protecting the public.

The discovery was made almost three weeks after FirstEnergy Corp. shut down the plant for refueling on Feb. 16, a date which utility officials had successfully negotiated after being threatened last November with what would have been the government’s first emergency shutdown order of a nuclear plant since 1987.

Now, a year after the decision to allow the utility to keep operating until early 2002 - and after a great deal of prodding by anti-nuclear activists, some members of Ohio’s congressional delegation and concerned residents - the NRC has put in writing its technical justification for making that compromise.

The report shows NRC officials suspected there might be some type of minor leakage with one or two of the 69 reactor-head nozzles. Uranium–enriched fuel rods are lowered and raised in the reactor to control the nuclear fission process.

But the NRC report contends the agency did not have a clue as to the extent of the corrosion from boric acid leaking out of the nozzles and onto the reactor head.

"To their credit, they based it [the report] on what they knew then," said David Lochbaum, a nationally recognized nuclear-safety engineer for the Union of Concerned Scientists..

But he added yesterday’s report did little to convince him that the NRC lived up to its mandate to ignore economic considerations and hold safety tantamount.

Mr. Lochbaum is one of several activists long convinced that FirstEnergy’s intensive lobbying efforts in Washington last fall persuaded the NRC to back off an immediate shut down as recommended by the staff.

Instead, the NRC let Davis-Besse keep running until Feb. 16, a date they view as an arbitrary halfway mark between the proposed Dec. 31 shutdown date and the normal refueling outage cycle that the company had originally planned for March 30.

"I think they just didn’t have the spine to back up their order to shut down the plant," Mr. Lochbaum said.

Paul Gunter, spokesman for the Washington-based Nuclear Information and Resource Service, agreed.

"These are the same excuses the agency offered previously," said Mr. Gunter, who lobbied the NRC for months to put its rationale in writing.

The NRC’s criminal investigation unit, as well as its Office of Inspector General, are among those still trying to determine what the NRC knew in advance of the shutdown and whether FirstEnergy illegally withheld photographs of the corrosion and other information so that the plant could remain open. FirstEnergy has denied such assertions.

Richard Wilkins, FirstEnergy spokesman, said the utility knew it had a leak but that it was "under technical specifications" allowed by the NRC.

"We assumed the risk to be minimal," he said.

Another internal probe by a special NRC panel called the "Lessons Learned Task Force" said in a report released in October that the agency failed to live up to a commitment to document its reasoning for the February shutdown date.

NRC spokesman Jan Strasma had little to say when asked why the explanation took a year to put in writing other than to state that yesterday’s report was not in response to any single occurrence.

"When we notified them [FirstEnergy] we were extending the time period, we said we would be providing the NRC’s rationale in separate correspondence. That was never done. So this completes the commitment we had in that letter and also responds to requests from various stakeholders," Mr. Strasma said.

NRC staff members had wanted Davis-Besse shut no later than Dec. 31 because they feared Davis-Besse might have a problem much more subtle and different than a thinned-out reactor head: tiny, circumferential cracks in reactor-head nozzles.

Those type of cracks had not been seen in the industry until the spring of 2001, when they were found at a South Carolina plant manufactured by the same company that designed Davis-Besse.

They are potentially more troublesome than vertical cracks because of their potential to weaken nozzles to the point they could pop off the reactor head like champagne corks, allowing radioactive steam to fill up the containment building, officials have said.

As it turned out, Davis-Besse had several axial cracks and at least two of the more dangerous circumferential type, according to laboratory results and government records.

The plant was one of a dozen identified by an industry group a year ago as being most susceptible to having circumferential cracks in its reactor-head nozzles.



More articles on this subject »
FirstEnergy lowers profit expectation 12/05/2002
Nuclear plant test scheme outlined 11/27/2002
Some not impressed by NRC’s mea culpa 11/21/2002
FirstEnergy reworks nuclear power unit 11/20/2002
FirstEnergy bid brings concern for deregulation 11/20/2002

Article Features »
Printer-friendly version
Forum on this topic
Email to a friend
View the Latest News index
Subcategories »
2002 Census

America Remembers

Davis-Besse

Accidents/Vehicular

City of Toledo

Courts

Crime

Elections

Environment

Fires

Higher Education

K-12 Education

Michigan News

Minority Issues

Obituaries - News

Ohio News

Other

Politics

Regional News

Religion

Suburban News

Transportation

War on terrorism

Weather

Zoo & Library







HOLIDAY CONTEST
Win a La-Z-Boy chair or a $100 gift certificate to participating retailers.

WINNERS LIST
Click here!





©2002 The Blade. Privacy Statement. By using this service, you accept the terms of our visitor agreement: Please read it.

The Toledo Blade Company, 541 N. Superior St., Toledo, OH 43660, (419) 724-6000
To contact a specific department or an individual person, click here.