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Hidden in plain view 12/01/02
As stark as a morgue photo, the picture from FirstEnergy Corp.'s files
captures a reactor in distress. Something is hemorrhaging atop the massive steel lid that covers the
radioactive core of the Davis-Besse nuclear plant near Toledo. The vivid color print, taken in April 2000, shows rust trails the hue
of dried blood spilling from inspection ports on the reactor's sloping
dome. The corrosion stains end in piles of white-brown debris at the lid's
edge. The loose clumps of dried acid are trapped there like fallen leaves
against a fence by the ring of huge bolts that locks the 80-ton cap in
place. Anyone who saw the image that has come to be known as the "red photo"
would have to question whether the lid - a vital safety barrier - was
damaged. "I would have concluded that a serious corrosion problem probably
existed" on the lid, said Digby Macdonald, an international corrosion
expert who directs Pennsylvania State University's Center for Advanced
Materials. But federal regulators never got that chance. FirstEnergy's nuclear division didn't share the 2-year-old photo with
senior Nuclear Regulatory Commission staffers last fall. It wasn't in the
batch of images the company provided the NRC in November 2001 as part of
FirstEnergy's successful campaign to convince the agency the lid was OK,
and to justify postponing a costly shutdown to inspect it. The photo didn't surface until April, on page 93 of a thick FirstEnergy
report. The document attempts to explain in hindsight how the company had
allowed boric acid sludge left behind by leaking reactor coolant to chew a
pineapple-size hole all the way through the 6.5-inch-thick lid. The unprecedented hole, found a month earlier, jeopardized the plant's
safety, rocked the nuclear industry and is expected to cost the company
nearly $400 million in repairs and replacement power purchases. The omitted photo is just one example of what regulatory officials say
are FirstEnergy's multiple failures over almost a decade to accurately
document and communicate what the company knew to be the worsening
condition of Davis-Besse's reactor lid. Those misrepresentations - especially during the crucial NRC review
last autumn - are the subject of an agency criminal probe. They also are
the subject of a new allegation by a watchdog group, the Nuclear
Information and Resource Service, which is calling for Davis-Besse's
license to be revoked. The NRC is reviewing that claim and may address it
in its ongoing investigation. The NRC already has determined that FirstEnergy's nuclear division
violated agency rules requiring that information be accurate and complete.
The company insists, without further explanation, that it did nothing
criminal. But if the inquiry under way by the NRC's criminal unit, the
Office of Investigations, verifies intentional wrongdoing, plant personnel
and FirstEnergy managers could find themselves answering to a federal
grand jury, or facing hefty civil fines. The findings also could affect the NRC's decision on whether or when to
allow Davis-Besse to resume making electricity. Neither the government nor FirstEnergy has been willing to say much
publicly about the records issue because of the investigations. In the
last few weeks, however, a picture of the evidence in the case and the
company's defense has emerged from newly released NRC reports as well as a
Plain Dealer review of thousands of pages of inspection documents, meeting
transcripts and briefing materials. While not contesting that their records were inaccurate and incomplete,
FirstEnergy officials have sought to portray the documentation problems as
benign miscommunications or misinterpretations rather than deliberate
attempts to deceive. They have said that evidence such as the "red photo"
that gave a more detailed indication of the lid's condition was available
if the NRC had looked hard enough. "It was there for the asking," said company spokesman Todd Schneider.
"Being our regulator, the NRC has full access to the plant, to our
documents, to just about every part of our operation." But that rationale sidesteps the key legal issue of why material in
FirstEnergy's files sharply differs from the rosy picture the company
painted for the NRC late last year to justify the reactor's continued
operation. "I think that's a little bit disingenuous," Brian Sheron, the agency's
associate director for project licensing and technical analysis, said. "We
were asking them to provide us with all the information to support their
argument to operate beyond Dec. 31. Apparently, we did not get
everything." The NRC itself is under fire from critics, including some members of
Congress, for allowing the plant to delay its lid inspection last fall.
Angry and embarrassed agency staffers say they made the right call based
on the information they had. "If we knew they had three or four inches of [acid] caked on top of the
head . . . that would have started the chain" of more intense questioning,
Sheron said. Had FirstEnergy disclosed that its inspections dating at least to 1998
had consistently found red, rusty lumps of acid on the lid - increasingly
large deposits that weren't fully cleaned off so the surface underneath
could be checked - "we would have challenged the licensee then and there
to explain what we were seeing," Sheron said. "If we didn't get a
reasonable explanation, we probably would have taken action to try to
force them to shut down." String of inaccuracies The string of inaccurate and incomplete Davis-Besse records that the
NRC has identified began in 1993. At that time, managers at the plant and at FirstEnergy's predecessor,
Toledo Edison Co., were debating whether to modify a platform that sits
atop the reactor lid. The structure helps support the dozens of control
rods that pass in and out of the reactor's core through sleeves, or
nozzles, in the lid to regulate the nuclear reaction. It also holds
insulation to contain the reactor's fierce heat. The problem with the service structure, though, was its close fit. At
the top of the lid, there was only a 2-inch gap between the lid's metal
surface and the insulation, making inspection of that area extremely
difficult. To check the lid's condition every two years during the plant's
refueling shutdown, inspectors attached a video camera to a pole and poked
it through one of the 16 small "mouse holes" that ring the service
structure's base. But it was hard to get the camera all the way to the top
of the lid. Davis-Besse's sister plants had begun cutting larger ports in the
structure to allow for better inspection and cleaning. In March 1990, a
Davis-Besse engineer recommended that the plant do the same after finding
boric acid residue from leaking coolant in several places on the lid. He
reminded his bosses of the acid's potential for harm. Managers finally decided in September 1993 that the modification wasn't
needed. The reason, according to the cancellation notice signed by four
high-level managers, was because "cleaning of the reactor vessel head
[lid] during last three outages [in 1990, '91 and '93] was completed
successfully without requiring access ports." That statement wasn't accurate, the NRC has determined. Agency
inspectors who reviewed Davis-Besse records from the 1991 and '93
refueling shutdowns found that workers had allowed acid deposits to remain
on the lid each time the reactor was restarted. FirstEnergy's own review this year notes that there are no records
indicating the lid was inspected at all in 1990. The FirstEnergy report
doesn't say what, if anything, the 1991 records show, but acknowledges the
company can't verify the effectiveness of the lid-cleaning done in 1993.
The record-keeping flaws at Davis-Besse continued in 1998. Plant
documents from that year stated that workers had cleaned acid buildup from
the lid, even though the company noted as an aside that its reactor's
manufacturer, Babcock & Wilcox, considered such deposits harmless.
Plant records also said inspections had shown the lid surface was free of
"any" corrosion damage. All three statements were incorrect, the NRC has found. A videotape of the 1998 inspection showed fist-sized clumps of red,
rusty acid on parts of the reactor lid, and Davis-Besse workers again
allowed some of them to remain, especially on the hard-to-reach top of the
dome. That precluded plant personnel from knowing, as they claimed to,
that the underlying metal was OK. In fact, the hole in the lid had started
its rapid growth that year, FirstEnergy surmises, in the very area workers
had left uncleaned. Also, none of the nine Babcock & Wilcox reports the NRC examined
contained the reassuring statement FirstEnergy had quoted: that acid
residue left on the lid wouldn't cause corrosion. There were multiple inaccuracies in Davis-Besse documents from 2000,
the NRC has found, most having to do with claims that the reactor lid was
rigorously cleaned and that inspection showed it to be unblemished. "Work performed without deviation," noted an April 25, 2000, order
signed by the reactor coolant system engineer detailing the lid-cleaning
activities. "Engineering displayed noteworthy persistence in ensuring
boric acid accumulation from the reactor head was thoroughly cleaned,"
trumpeted a July 7, 2000, report by the plant's quality assurance unit.
None of it was true. As FirstEnergy acknowledged in reports to the NRC
this year, Davis-Besse personnel were under intense pressure to stay on
the tight work schedule during the refueling outage so the plant could
resume making electricity - and money - as soon as possible. Workers examining the lid at the start of the 2000 outage found
rock-hard, "lava-like" piles of acid that clogged some of the mouse holes
and hindered the video camera's path. They did some cleaning, but with
time running out, managers decided to stop, leaving some acid clumps in
place and part of the lid unchecked. Contrary to policy, they didn't do a
written evaluation to justify their actions. Eighteen months later, when FirstEnergy officials were pressing the NRC
to postpone the mandatory lid inspections that most other plants were
doing to look for possible nozzle cracks, they assured the agency their
lid was in good shape. But as the NRC would later discover, the evidence
the company provided was selective and misleading. In letters and in-person briefings to the NRC staff at the agency's
Rockville, Md., headquarters, company officials mentioned having found
"some" boric acid in past inspections. But they didn't reveal the
alarmingly rusty characteristics and amount of the acid residue - by this
time nearing 900 pounds, they later found out - that had been accumulating
for years. In one meeting, for example, FirstEnergy nuclear division president
Robert Saunders "said he knew there was some light dusting of boron in
certain spots. But he said he was not concerned that was from major
leakage," recalled the NRC's Sheron. And in an Oct. 17, 2001, letter, FirstEnergy nuclear division support
services director L.W. Worley told NRC staffers that the lid was cleaned
in 1996. He added that re-reviews of the videotapes from that inspection
and ones in 1998 and 2000 "did not identify any leakage in the . . .
nozzle-to-head areas that could be inspected." When NRC staffers continued to push for a shutdown by Dec. 31,
FirstEnergy officials volunteered to fly to Rockville with the inspection
videotapes so NRC staffers could see for themselves. But the company
didn't show any tapes that depicted the masses of rusty acid accumulated
at the center of the lid, according to the NRC's subsequent interviews
with staffers who attended the meeting. "The NRC staff members recollected that they were shown freeze-frame
video images that depicted inspectable nozzles, i.e. free of significant
deposits," an NRC task force reported last month. "The nature and extent
of boric acid deposits remaining on the [lid] . . . were not disclosed."
The NRC has always been heavily dependent on the candor of the
utilities it regulates. There are 103 commercial nuclear reactors in the
United States, each a highly complex machine with dozens of operational
issues per day that require attention and generate thousands of pages of
paperwork. Even in the best of times, the agency has only a dozen or so people
monitoring the day-to-day operations of an individual plant - two or three
on-site inspectors and the rest at regional offices or at headquarters.
Because of its staffing level, "the NRC doesn't count every thread on
every bolt; we focus on things that are safety-significant," the agency's
Sheron said. "We poke, we probe, we ask questions. But for the most part,
we rely on the licensee. Our whole regulatory process is based on trust."
The agency's oversight of Davis-Besse was particularly vulnerable at
the exact time the hole in the reactor's lid was forming and growing, in
the late 1990s. The resident inspector's post at the plant was vacant for a year; the
job of senior project engineer for Davis-Besse at the NRC's Midwest
regional office was left empty for 20 months. And there were serious
problems at other area reactors that required attention, so the amount of
time the agency spent on inspections at Davis-Besse plummeted to an
eight-year low. However, the NRC's own shortcomings don't explain FirstEnergy's
repeated failures to disclose what it knew. Legal review After news of the NRC's probe of possible criminal wrongdoing leaked
this spring, FirstEnergy asked one of its law firms to review staff
activities at the plant during the past decade. The company won't discuss or release the findings, but an executive
told stock analysts in September that while Davis-Besse managers had made
poor decisions in operating the reactor and dealing with federal
regulators, the law firm found no behavior "which would rise to criminal."
Instead, in numerous filings and meetings with the NRC to explain
itself, FirstEnergy has depicted former Davis-Besse managers as
production-obsessed and out of touch with the plant, and workers as being
naive about the potential for boric acid deposits to harm the reactor lid
if left in place. Only wet boric acid posed a corrosion threat, and plant
personnel wrongly thought that, once the steel lid's searing heat
instantly dried the leaking coolant, the acid deposits left behind
couldn't get wet again. But if Davis-Besse personnel truly believed the acid buildup was
harmless, why not acknowledge its presence? Why say or imply that it had
been fully cleaned away when it hadn't? "That is one of the standards problems we're trying to correct at the
plant - that cleaning the head back then meant cleaning as much as you
could, not the entire head," said FirstEnergy's Schneider. "That's about
all I can say on that. Those issues will come out in the investigation."
FirstEnergy has fired, transferred or reprimanded some senior employees
in connection with the hole in the lid. But it is mum on whether those
moves, which included the departure of nuclear division Vice Presidents
Guy Campbell and Howard Bergendahl and engineering director John Wood,
were because of the record-keeping inaccuracies. The NRC's Sheron said FirstEnergy nuclear division President Robert
Saunders told him the disciplinary steps were a consequence of its law
firm's review. "I don't think a company would fire somebody if it
concluded they hadn't done anything wrong," Sheron said. FirstEnergy's Schneider has said the company expects to be fined for
its overall lapses, but that the management changes and renewed focus on
safety should be enough to regain the trust of the NRC and the public.
A national nuclear watchdog group disagrees. Concerned that the NRC
will accept superficial changes at Davis-Besse and not push for
fundamental reforms, the Nuclear Information and Resource Service recently
filed a complaint with the NRC. It alleges that FirstEnergy records
contained false and inaccurate statements about the Davis-Besse reactor
lid, and that the company's analyses of the event have failed to explain
why. The NRC has assigned the allegation to a review board, and, if it's
deemed serious enough, it could be incorporated into the Office of
Investigation's ongoing work. Davis-Besse "should have its operating license revoked," said Paul
Gunter, director of NIRS' reactor watchdog project and the author of the
complaint. "Our concern remains that the NRC is going to go along with
this plan to just replace managers at Davis-Besse as the solution to
underlying problems with the management culture that places production
over safety." With Davis-Besse aiming to finish its repair work by late January or
February, it's possible the NRC may have to decide whether to let the
plant resume operating before the agency's criminal inquiry is complete.
Although it may not have the final report in hand before restart, the
special NRC panel overseeing Davis-Besse's rehabilitation will have a good
idea of what the findings will be, said its chairman, Jack Grobe. The
decision will hinge on whether FirstEnergy has corrected whatever
deficiencies the probe finds. "We'll have to have confidence in the plant personnel" before letting
Davis-Besse power up again, Grobe said. "This is a critical element." For full coverage of Davis-Besse, go to www.cleveland.com/davisbesse/
To reach these Plain Dealer reporters: jmangels@plaind.com, 216-999-4842 jfunk@plaind.com, 216-999-4842
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