GLEN ROSE - Routine inspections at the
Comanche Peak nuclear power plant failed to detect a damaged steam
generator tube that later ruptured, forcing a shutdown in September,
according to a federal report released Tuesday.
The flaw in the tube was "clearly identifiable and missed" about
18 months ago by workers for TXU Energy, the plant's owner and
operator, according to the preliminary findings of a special
inspection team of the Nuclear Regulatory Commission.
The error, termed an "apparent violation" in the report, did not
pose a safety or public health risk, NRC officials said. They
praised the company for taking "appropriate and conservative" action
in response to the leak.
"Consistent with putting safety first, we shut the plant down,"
C. Lance Terry, TXU's principal nuclear officer, said at a meeting
near the power plant about 50 miles southwest of Fort Worth.
Terry said the small leak was well below NRC guidelines and TXU's
more conservative guidelines.
The NRC is still evaluating the risk associated with the error,
said Roger Hannah, NRC spokesman.
"In all likelihood, there wouldn't be a civil penalty but there
could be additional oversight or inspections," Hannah said.
The steam generator tubes carry superheated, radioactive water
from the reactor's core to heat nonradioactive water, creating steam
to run turbines to produce electricity.
There are 4,578 tubes in each of the reactor's four steam
generators.
The September incident was the first time a tube has leaked at
either of Comanche Peak's two reactors.
But the Unit I reactor that went on line in 1990 has had its
share of problems with cracked and corroded steam tubes that have
been repaired or plugged, company officials said.
There were no tube problems in the reactor's first five years of
operation. But since 1995, about 700 damaged tubes have been
identified and plugged -- taken out of service -- before they
leaked, said James Kelley, TXU's nuclear engineering vice
president.
Leaking and cracked tubes have been long-standing problems at
plants that were built with Westinghouse-engineered pressurized
water reactors. The Westinghouse system has been installed in both
commercial nuclear power plants in Texas, Comanche Peak and the
South Texas Project.
The thin tubes -- made of a stainless steel alloy called Inconel
600 and designed to last 40 years -- are scheduled to be inspected
every 18 months, when the reactor is refueled.
In some cases, they have cracked and leaked within 10 years of
installation, according to NRC records.
The most recent inspection of Unit 1, in October, found more than
660 damaged tubes, nearly equal to the total number of damaged tubes
found in the past 12 years.
The tubes were repaired with sleeves instead of being taken out
of service, which would have caused the plant to lose efficiency,
Kelley said.
Terry told the NRC that he is confident that Unit 1 can operate
for another 18 months, but nuclear industry critics warn that the
tube problem needs greater attention.
"If a tube breaks and ruptures, it could cause a domino effect,
breaking additional tubes," said David Lochbaum, a nuclear engineer
who works with the Union of Concerned Scientists.
"It wouldn't take more than 10 broken tubes to let more water
flow out than you can put back in, jeopardizing the ability to cool
the reactor core," he said.
Steam-tube problems and the cost of replacing entire systems
contributed to the early retirement of nuclear power plants in
Oregon, Maine and Illinois, said Jim Riccio, a nuclear policy
analyst with Greenpeace.
At least 19 steam-generating systems have been replaced at
nuclear plants for $100 million to $200 million per plant, records
show.
The South Texas Project replaced its steam generators in the past
two years.
"It [Inconel 600] is one of the great failures in terms of
selecting a material for nuclear power plants," Riccio said.
The tube problem has led to at least 14 lawsuits against
Westinghouse, all of which have been settled out of court with most
court documents sealed.
Kelley said TXU has not made a decision on whether to replace
Unit 1's four steam generators, which would cost about $150 million.
Delivery of new steam generators could take about six years, he
said.
Dwight Chamberlain, the NRC's regional director of reactor
safety, said the agency is analyzing the Comanche Peak problem to
see if it can learn something about the detection of flaws.
The inspection team expects to issue a final report in about a
month, NRC officials said.
After the September leak, Unit 1 was shut down for 50 days to
repair the tubes and for refueling.
The unit has been started and stopped twice since Nov. 15, once
for a potential valve problem and the second time because of a leaky
weld at a control rod.
Unit 1 remains out of service but is expected to be put back in
service in a few days, company officials said.