Home     News     Communities     Classifieds     Cars     Jobs     Customer Service
 
Home
News
  Local News
  Local Sports
  Nation/World
  Ohio News
  Obituaries
  Opinion
  Technology
  Space & Science
  Weather
 
Communities
Classifieds
Cars
Jobs
Customer Service
Network Newspapers
  The Advocate,
  Newark
  Chillicothe Gazette
  Coshocton Tribune
  The Fishwrapper
  The Granville
  Sentinel
  Lancaster
  Eagle-Gazette
  The Marion Star
  News Journal,
  Mansfield
  News-Messenger,
  Fremont
  The Pataskala
  Standard
  Telegraph-Forum,
  Bucyrus
  Times Recorder,
  Zanesville

  Wednesday, December 11, 2002

 Local News


FirstEnergy officials say difficult hurdles remain


Staff writer


CARROLL TOWNSHIP -- Even as FirstEnergy officials introduced industry-leading ideas Tuesday afternoon, they are still faced with major hurdles in upcoming reviews of technical issues at the Davis-Besse Nuclear Power Station.

Those technical reviews pose such a potential for problems that the utility has tentatively scheduled a meeting with the Nuclear Regulatory Commission to touch on only those issues.

The NRC met with FirstEnergy officials Tuesday as part of a monthly progress report on the Davis-Besse plant, which has been off-line since February. Workers in March found an unprecedented amount of corrosion on the reactor head from boric acid leakage.

Jack Grobe, head of the NRC review panel watching the progress at Davis-Besse, said during the regular meeting that workers have only begun to identify technical issues regarding calculations involving critical safety equipment.

The calculations may or may not affect system operations at the beleaguered plant, but Grobe said he would like to hear greater detail into the reviews at a meeting tentatively scheduled for Dec. 23.

"The standard that we need to come to as we approach restart is that all systems are operating correctly," Grobe said. "We need to know that before we recommend restart."

Grobe did, however, offer compliments by the way of saying officials have shown steady progress since the last meeting. He tempered that praise, though, by adding that he and his panel members would like to see more proof that management is trying to change the safety culture at the plant.

And while officials said they were still working on that aspect -- probably one of the largest tasks they have -- they also talked about three actions that would make Davis-Besse an industry-wide leader in leak detection and emergency systems.

Those three actions are:

*Modifying the containment sump, which floods the containment area with coolant water and recycles it in case of a loss of coolant accident. The modification would expand the square footage of a screen that sits on top of the sump from 50 square feet to 1,200 square feet.

That is expected to be completed before the plant restarts.

*Implementing a leak rate program to catch even the smallest leaks as they occur, establishing a new industry standard.

*Installing a leakage detection system called Flus Sensors, which originated in Europe. The system detects moisture content in the air, which could be an indicator for a leak.

That system is expected to be installed before the plant restarts as well.

Those improvements will help in the future, but Davis-Besse officials are still investigating the cause of boron deposits on the bottom of the reactor head found in October.

When workers found the initial corrosion in March, it was on top of the reactor head, and was caused by cracks in nozzles there. Plant officials believe some of that leakage may have dribbled down the side of the reactor and pooled at nozzles on the bottom.

However, they have not completely ruled out leakage from bottom nozzles, although officials said Tuesday the bottom nozzles are not nearly as susceptible to cracking as the top ones.

FirstEnergy official Jim Powers also offered an alternate explanation. He said during refueling, temporary seals are placed on the reactor while flowing coolant water in. It is possible those seals leaked, causing the deposits on the bottom of the head.

There are "flow trails" to the bottom of the head, but FirstEnergy official Bob Schrauder added that some nozzles had deposits on them that were not in the flow path.

Samples have been taken from those nozzles, as well as other parts of the reactor head. And officials want to reheat the plant without a nuclear reaction for seven days to inspect the nozzles for leakage.

That could take place at the end of January.

Originally published Wednesday, December 11, 2002

Home | News | Communities | Classifieds | Cars | Jobs | Customer Service


    Contact Us | Subscribe | Place an ad
Copyright ©2002 News Herald. All rights reserved.
Use of this site indicates your agreement to the Terms of Service
(Terms updated 08/10/01)