FirstEnergy's Beaver Valley Unit 1 nuclear plant shut down
suddenly Monday afternoon, releasing a small amount of radiation
into the atmosphere.
FirstEnergy now has two of its four nuclear reactors off-line.
The other is Davis-Besse, which has been out for more than a year. A
Nuclear Regulatory Commission report released Tuesday said
FirstEnergy's troubled Davis-Besse plant was just a year or two away
from a serious accident when a safety inspection last year unearthed
unexpected reactor damage.
The Beaver Valley complex, which holds two nuclear reactors, is
on the Ohio River near Shippingport, Pa., not far from the West
Virginia and Ohio lines.
At Beaver Valley, tritium, a radioactive byproduct of the
reactor, was vented along with steam into the atmosphere,
FirstEnergy and the NRC said. The amount of radiation released, well
under a millirem, was less than 1 percent of the amount of radiation
the plant is allowed to put out into the environment in a year's
time, the Akron utility said. The tiny amount of radiation was
detectable while it was inside the plant; the amounts were too small
to be detected in the atmosphere outside the plant because it
dissipated, FirstEnergy spokesman Todd Schneider said.
Workers bumped scaffolding into a steam line valve, forcing the
valve to close and shut off a steam line that leads to the plant's
power turbine, Schneider said. A diaphragm in the valve needs to be
replaced, he said.
The workers were getting the plant ready for a refueling outage
that is scheduled to start next month, Schneider said.
The NRC said the gaseous tritium would have little to no effect
on the public. Most people are exposed to 300 to 360 millirems of
radiation a year from natural and man-made sources, NRC spokesman
Neil Sheehan said.
The Beaver Valley release amounted to 0.000000512 millirems, he
said.
Repairs are under way at Unit 1, which likely will be back online
by the end of the week, Schneider said. ``The plant shut down as
designed. All of the safety systems worked.''
Beaver Valley Unit 1 automatically shut down at 3:48 p.m. Monday
after it detected low steam line pressure. The plant shift manager
declared the shutdown an ``unusual event'' at 4 p.m. while also
saying the unit was stable. An unusual event is the lowest of the
NRC's four emergency classifications. The unusual event designation
was lifted at 5:35 p.m. Monday, according to the NRC.
``To be conservative, they declared it an unusual event,''
Sheehan said.
Davis-Besse details
The NRC report on Davis- Besse said that under a worst-case
scenario, in which boric acid continued to quickly chew out a larger
cavity into the six-inch-thick carbon steel reactor head, a loss of
coolant accident could have happened this year or in 2004.
As a result of the boric acid damage, the NRC report classified
the Davis-Besse incident as ``highly safety significant'' and gave
it the agency's worst color-coded safety rating, red. The report and
safety rating followed a nearly yearlong investigation into what
caused boric acid to eat a large cavity nearly all the way through
the top of the nuclear reactor and start a second, much smaller
cavity.
The red designation will not affect FirstEnergy's efforts to get
Davis-Besse ready to restart by mid-April, Schneider said. But the
designation will be a factor in deciding the size of a civil penalty
the utility expects to pay. The NRC will determine when Davis-Besse
will be allowed to restart.
FirstEnergy will not contest the red designation, Schneider
said.
David Lochbaum, nuclear expert for the Union of Concerned
Scientists, said the NRC's red designation ``is more historical than
it is instructive.''
Surprising damage
The NRC took nearly a year to determine the red finding because
it never expected the kind of damage found March 5 at Davis-Besse
and had to revamp methodologies and formulas in trying to figure out
how boric acid corroded the top of the reactor, Lochbaum said.
``That complication messed up their mathematical models,'' he
said. ``They had to sit down and essentially start with a clean
slate.''
The NRC report said that the creation of one large boric acid
cavity significantly increased the chances for a loss of coolant
accident, in which high pressure reactor coolant jets out of the
reactor and into the massive containment building.
There was no loss of coolant accident or release of radiation at
Davis-Besse, which is in Oak Harbor along the Lake Erie shoreline. A
FirstEnergy report released earlier this year said that an emergency
sump system, designed to keep the nuclear fuel from melting in a
loss of coolant accident, was defective and could have been clogged
by debris and rendered unusable.
By luck only, a thin interior lining of stainless steel held
coolant inside the reactor vessel and prevented an accident, the NRC
report said.
The report also reveals that the NRC staff has problems
understanding exactly what damage the boric acid corrosion would
have caused at the reactor.
At the time the damage was found, it did not appear that the
plant was in imminent danger of a loss of coolant accident, the
report said.
Other problem plants
This is the third time since 1999 that the NRC has determined a
plant merits a red designation, NRC spokesman Jan Strasma said. The
NRC gave similar designations to the Indian Point II plant in New
York and Point Beach plant in Wisconsin, he said.
The NRC expands its inspections and oversight at troubled plants
after they get a red designation, Strasma said.
In Davis-Besse's case, those expanded efforts were under way
shortly after the boric acid corrosion was first found.