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News
Besse operators face NRC rebuke 08/01/03
The Nuclear Regulatory Commission said yesterday it is preparing to
cite the Davis-Besse nuclear power plant's operators with the agency's
second-most severe finding for failing for decades to correct conditions
in the reactor building that could have caused emergency safety systems to
fail during an accident. The issue has been on the bubble for months - that paint chips and
fibrous insulation could have plugged the plant's emergency sump after a
coolant-loss accident, starving emergency pumps designed to put water back
into the reactor and keep the nuclear core from melting. The NRC report notes that Davis-Besse managers knew as early as 1976 -
a year before the plant opened - that the paint used to coat the reactor
building's interior walls and much of its equipment might not be able to
stand up to a geyser of steam if a major pipe were to break or the reactor
itself leak. Yet they did nothing. The agency itself issued a letter to Davis-Besse and operators of
similar reactors in 1998 warning that the paint could peel off and clog
the sump screens. Davis-Besse initiated several efforts to fix the problem
but apparently never followed through. Plant owner FirstEnergy Corp. has 10 days to object to the citation -
that it operated Davis-Besse for 26 years with a substantial risk that its
radioactive core could have been seriously damaged in an accident. A FirstEnergy spokesman said last night that the company would not
object to the findings - and that in any case it had already fixed the
problems by rebuilding the sump screens at a cost of nearly $4 million and
removing old paint and insulation from equipment and from the interior
walls of the reactor building. The agency uses a four-color system to express the safety significance
of its citations, with green being the least-significant violation and red
the most serious. In this case, the NRC believes the violation deserves a
yellow finding - one step below red - because the safety of the plant was
compromised. Consequences of such a ruling are normally stepped-up NRC oversight at
a plant, but since the agency already has numerous teams of inspectors
there, there are no immediate consequences, said Jack Grobe, head of the
special agency panel overseeing the company's efforts to fix the troubled
facility. Davis-Besse has been shut down since February 2002 for an expected $258
million in repairs by year's end resulting from NRC-mandated inspection
that turned up a large corrosion hole in the reactor's heavy carbon steel
lid. Only a thin stainless steel liner was keeping the super-heated
radioactive coolant from bursting through the lid. The reactor operates at
pressures of more than one ton per square inch. The yellow finding is further evidence that the company cannot be
trusted to restart and safely operate the power plant, said Paul Gunter of
the Nuclear Information and Resource Service, a reactor watchdog group.
The agency's decision to assign a yellow - rather than a red - finding
to the sump screen deficiency is also questionable, said David Lochbaum,
nuclear engineer with the Union of Concerned Scientists. NRC engineers calculating the chances that an accident clogging the
sump screens could increase the danger of a meltdown occurring used
generic industry probability factors rather than numbers that would have
taken into account the unprecedented corrosion in Davis-Besse's reactor
lid. "The hole in Davis-Besse's reactor head made it more likely that the
plant would have had a . . . loss-of-coolant accident," said Lochbaum,
saying the generic industry numbers were too lenient. Grobe confirmed that the calculations were done using industry-standard
probability numbers because FirstEnergy decided not to do the complicated
analysis - though it had twice promised it - of how much paint and
insulation would have been blown off equipment and walls had the corrosion
hole burst. Asked why he did not simply demand the analysis, Grobe said he believed
that the expensive and time-consuming analysis would have diverted
resources and manpower that the company ought to be using to fix the
plant. The NRC also listed a number of management and worker problems that
either the company or the agency's teams of inspectors spotted in recent
weeks while observing restoration of the Toledo-area plant. Those included improperly tightening bolts on machinery, leading to
damage when it was tested and leaving open valves during a procedure to
put new coolant into the reactor, flooding the plant's turbine building
with three inches of water. The agency said the foul-ups were not of high safety significance and
therefore would be classified as "green." But they have not gone
unnoticed, said Grobe, as the company pushes toward asking permission for
restart. "Their performance is not at a level that would meet NRC
requirements," he said, "and we will continue to monitor. "Am I confident (FirstEnergy can operate the plant safely)? I am only
confident in what I observe. As of now, I have observed that they haven't
yet demonstrated sustained improvement in this area." To reach this Plain Dealer reporter: jfunk@plaind.com, 216-999-4138
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