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News
NRC focusing on Davis-Besse operators 10/08/03
Camp Perry- If the managers of the Davis-Besse nuclear power plant
thought the nearly completed - and so far successful - leak test of the
reactor meant they will soon get permission to resume making electricity,
they learned yesterday they were mistaken. The Nuclear Regulatory Commission's special panel overseeing the
efforts of plant owner FirstEnergy Corp. to renovate the Toledo-area
reactor is just as interested in people issues as it has been in hardware.
"At this point in a plant's recovery effort, it is easy to see the
light at the end of the tunnel from a hardware perspective," committee
chairman Jack Grobe told company officials at the end of FirstEnergy's
monthly public briefing. "It is harder on what I call the software"
issues. Grobe's comments came after plant officials listed a number of
technical problems they believe workers will have fixed by early November.
But Grobe wanted to know what dates the company is targeting to finish
a new system it uses to correct problems as they develop and to improve
the performance of its reactor operators - who twice created problems for
themselves during the leak test. "We have a game plan on the corrective actions," said Lew Myers, chief
operating officer of FirstEnergy's nuclear operating company. "From the
operations standpoint, it would be unfair to say all the steps we will
take," he added. "But we will nail it." At the briefing, Vermilion resident Joseph Korff said remarks from
Myers and other top managers did little to relieve his concern about the
company's fitness to operate a nuclear plant. In response, Grobe again stressed that the NRC, not FirstEnergy, will
decide when Davis-Besse will resume making electricity. "It doesn't matter, and has not mattered throughout this process, what
dates FirstEnergy puts up," he said. "You can rest assured that this panel
will not make a recommendation until we think the plant can operate
safely." Oversight panel member Christine Lipa noted that of the 31 items on the
NRC's "restart checklist," 18 are still open. Myers' staff reported on remaining equipment problems, on problems
uncovered during the leak test and on how well the plant's operators and
other staffers worked together during the 13 days they heated up the
reactor to full operating pressure by non-nuclear means to test it for
leaks. The reactor and its cooling system showed a leak rate of just 0.006
gallons per minute, or 0.728 teaspoons, the best in its history, said Greg
Dunn, manager of work control. "And those leaks were properly identified,"
he said. The NRC allows plants to have unidentified leaks of up to one gallon
per minute. The leak of boric acid-laced coolant that ate a hole in the
reactor's old lid was less than that. Davis-Besse's reactor and cooling
system contains nearly 90,000 gallons of coolant. All told, workers checked about 1,342 connections and valves, Dunn
said, and found 161 mostly minor problems. Of those, just 61 remain to be
repaired or adjusted. Inspectors did not observe any leaks above the new
lid nor any leaks in the reactor's bottom. A robotic camera was still
inspecting the bottom yesterday. Operations problems observed during the pressure test have disturbed
both the NRC and Davis-Besse's managers. Operators were not well briefed,
the written procedures were not well written, and operator performance was
not up to industry standards, reported Mike Roder, manager of plant
operations. "I am deeply disappointed in operator performance," he said, "but
confident the steps we have taken will straighten it out." Among those steps: hiring a new training manager, interviewing all
operators to assess their strengths and weaknesses and reassigning
operators to new crews. Staff is also conducting a "root cause" inquiry
into how operators failed, he said. One of the "human performance" tests Davis-Besse conducted during the
pressurizing was to have observers watch workers for signs they had
learned how to solve problems and work without fear of reprisals from
bosses. Those observers were themselves the focus of a team of outside
industry executives who tried to assess how objective they were, said Rick
Dame, supervisor of reliability. The outside team noted that the in-house observers were not as critical
as they should be and that newly hired managers were more self-critical -
a trait appreciated by the NRC - than long-time employees. They also noted
that during the course of the test, these new managers began coaching the
older staff to take on the same traits. Those were the preliminary findings. Dame said he is preparing a
comprehensive report. During the nearly six hours of hearing yesterday, NRC Deputy Executive
Director Samuel Collins sat in the audience, taking notes. "I am just
gathering information," Collins said afterward. "Nothing I heard today
surprises me. No date was announced for restart. And we are not here to
push them." To reach this Plain Dealer reporter: jfunk@plaind.com, 216-999-4138
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